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SO what did you you do with your Stag today?
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Originally posted by milothedog View PostProbably the box unfortunately mate, it was probably damaged with that incident in your Garage. If I were you I would shove a bottle of additive in it, I've heard good things about an this one. http://www.ebay.co.uk/itm/Lucas-Tran...25.m3641.l6368, cheap enough to see if it improves things and It should buy you a bit of time given the amount you use the car.
Ian.
Checked the trans fluid and put the additive in, it took a few hundred mile but it certainly improved it and it is now as good as a BW 35 will be.
Nigel
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Originally posted by HersnotHis View PostLast day or so I have had wiper motor on bench. Was only going one speed and parking only occasionally and then not properly
Removed from car and dismantled and found short between fast/slow terminals and intermittent sticking of park switch as the poylester post was bent. Removed and cleaned park switch but could not straighten plastic park switch post which still stuck intermittently. Considered heating options to assit with straightening and eventually tried dribbling boiling water over post whilst straightening - worked a treat!
Having fully re-assemlbled and re- installed to car and connections - nothing?? After a lot of testing established that 12V was delivered to the wiper unit and more significantly at the fuse.
However after a bit of head scratching and evaluaton I concluded from the wiring diagram that as washer also did not work the general 12V supply was compromised.
What I found that was the fuse mounting was able to deliver 12V in an unloaded condition it would not deliver any significant current if a load was placed. (Surprising? Mislieadng etc.)
Cleaning fuse holder has solved most.
HTH somebody!
H
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Took the kids to Karate today, fixed the leccy aerial, finished fitting the boot carpet, washed it and put some more Dynax S50 in various cavities.
Looked at remaking my passenger door card back board but couldn't be bothered!
Jason
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Sorted my fuel pump today.
Original (say original, 30 year old Moprod electronic) has a crack in the plastic head so was spraying fuel out, not good.
Bought another (new old stock), and it wouldn't run with the voltage drop without the engine running...but you can't start your engine without fuel!
So made a good one between them, new body, old motor.
Tomorrow if time, change tubular exhaust manifold gaskets on near side due to blowing gasket.
Should then be good to go!Mike.
74 Stag (Best Modified 2007), 02 Maserati 4200, 17 BMW M140i, 00 Mitsubishi Pinin
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Started out calibrating speedometer against sat nav. With stooligan Nasty vibration issues at 60 mph+ Repositioned rear hight of gearbox Checked drive shafts play detected new shafts required bit of a pain as mine are staked. Lucky that I purchased a pair of circliped drive shafts and hubs at the Norfolk national meet
Cheers Glenn
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